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Related: Editorials & Other Articles, Issue Forums, Alliance Forums, Region Forums12 dead after engine fell off UPS plane that crashed and exploded in Kentucky
By BRUCE SCHREINER, HALLIE GOLDEN and DYLAN LOVAN
Updated 8:28 PM EST, November 5, 2025
LOUISVILLE, Ky. (AP) A UPS cargo planes left wing caught fire and an engine fell off just before it crashed and exploded after takeoff in Kentucky, a federal official said Wednesday, offering the first investigative details about a disaster that killed at least 12 people, including a child.
Finding survivors seemed unlikely as first responders searched the charred area of the crash at UPS Worldport, the companys global aviation hub in Louisville, Gov. Andy Beshear said. The inferno consumed the enormous aircraft and spread to nearby businesses.
After being cleared for takeoff, a large fire developed in the left wing, said Todd Inman, a member of the National Transportation Safety Board, which is leading the investigation. The NTSB will now try to determine what caused the fire and why the engine fell off. It will likely take investigators more than a year to answer those questions.
https://apnews.com/article/ups-cargo-plane-explosion-louisville-deaths-af12da7f8611bad0bf0cb664de189250
And there is this reporting about the plane.......
https://news4sanantonio.com/news/local/louisville-ups-crash-plane-had-recent-maintenance-in-san-antonio-records-show-travel-mail-local
If the engine separated from the aircraft they are going to look for the pylon bolts............
Ocelot II
(128,249 posts)due to an unapproved maintenance procedure. The plane crashed shortly after takeoff. It appears that the L engine on UPS plane was already on fire when it fell off, or the separation caused the fire.
TheBlackAdder
(29,842 posts)Some executive guy in first class pressured her into having fun with him. She rebuffed the man and he reported her to HR to get her fired. She didn't complete her regular flight that day as she had to stop off at DFW. When she went to HR, after questioning her and giving her a hard time because she upset a customer, she quit. This was back in the day and the female flight attendants were expected to take abuse. And the rest is history. She was a mess for a while because all of her friends perished.
If I remember from one of my aviation college courses, Aircraft Powerplants, there were just three main bolts holding the engine, two for downward and one for lateral forces. The lateral force bolt failed causing the other two to shear.
malaise
(291,003 posts)So glad for her
TheBlackAdder
(29,842 posts)Ocelot II
(128,249 posts)What an awful experience! Some asshole gropes her; she quits because management thinks FAs should have to put up with being groped, and the flight she left to go to HR crashes. Yeah, I'd be freaked out too.
https://en.wikipedia.org/wiki/American_Airlines_Flight_191
turbinetree
(26,770 posts)and they did not install those pylon bolts correctly.............3 if memory serves me correctly 2 in the front and 1 in the back for lateral force that is going to be a problem for the people that worked on that plane , if there was an engine change.
GE and Boeing are very specific on the procedure to do that change and it normally takes about 8 hrs to 12 hrs to do if memory serves me correctly to do .
You have to remove a lot of the cowling and such and disconnect the electrical harshness and hydraulic lines and fuel lines and then to place the engine cradle and hoist that cradle up and set the engine in the cradle by releasing the bolts that are made of Inconel with AC on jack stands.
There are also reports that there was a repair to the fuel system fuel tanks.
There are many factors..............but this is extremely sad..........
Ocelot II
(128,249 posts)If the forklift had been positioned incorrectly, the engine/pylon assembly would not be stable as it was being handled, causing it to rock like a seesaw and jam the pylon against the wing's attachment points. Forklift operators were guided only by hand and voice signals, as they could not directly see the junction between the pylon and the wing. Positioning had to be extremely accurate, or structural damage could result. Compounding the problem, maintenance work on N110AA did not go smoothly. The mechanics started disconnecting the engine and pylon as a single unit, but a shift change occurred halfway through the job. During this interval, even though the forklift remained stationary, the forks supporting the entire weight of the engine and pylon moved downward slightly due to a normal loss of hydraulic pressure associated with the forklift engine being turned off; this caused a misalignment between the engine/pylon and wing. When work was resumed, the pylon was jammed on the wing, and the forklift had to be re-positioned. Whether damage to the mount was caused by the initial downward movement of the engine/pylon structure or by the realignment attempt is unclear. Regardless of how it happened, the resulting damage, although insufficient to cause an immediate failure, eventually developed into fatigue cracking, worsening with each takeoff and landing cycle during the eight weeks that followed. When the attachment finally failed, the engine and its pylon broke away from the wing. The structure surrounding the forward pylon mount also failed from the resulting stresses.
turbinetree
(26,770 posts)was attached and lifted the entire cradle and engine to the wing or vise a versa to remove the engine being taken off. We had an engine change kit that we put in a LD Container specifically for engine changes if we had to fly to another airport. When we were attaching the engine to the pylon we had to make sure that we did not exceed the torque loads to the bolts.
And after we got it all together we took the plane out to to do an engine run
SoFlaBro
(3,722 posts)durablend
(8,757 posts)Orrex
(66,376 posts)Rec
Ocelot II
(128,249 posts)destined for the White House, he wouldn't.